CMM machine AMC staff did not turn up in the morning. Terminal box connection process was inspected in the Shop # 23
Loco 30049 WAP5 in the test and trial line was inspected, one of the operating rod was not working , same was reported to Dy.CME(ELF) .
Despite
reminding in PPM there are movements without movement slips in from Shop #17
and 18.
Regarding Railway Board’s letter dated 29.11.11, inspection was carried out in the wheel assembly shop (Shop# 09 ), and fitment of 8 bolts was inspected .
These
axle end tightening bolts were of CAPARO make(not approved), oversized by 5mm (
90 mm instead of 85 mm) but were tightened properly ( with 80nm torque wrench).
8
holes are tapped at both ends of the axle.Tapping of holes was done with the
standard tap. In order to accommodate
over-long stud/bolts, depth of the tap was increased hence tightening was
ensured.
CMM
machine was operated by Sh Duddel (Only artisan who knows to operate this
machine) of TM shop today . Labyrinth
measurement was tried but machine could
not work properly. Shop supervisor asked AMC staff to attend tomorrow.
This
machine was out of order due to belt broken and was reported made fit day
before yesterday only.
PPM
was attended in the afternoon.
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